It was the best of times, it was the worst of times…
You think I’d have more to say about my first few outings in the T-bird. Well, I do actually, its just I’ve been swamped with a grueling schedule, and haven’t had a chance to sit and reflect. What better time to do so than after midnight on an exhausting race weekend. (I know, I make no sense)
[cue drumroll] So, finally, after a year and a half out of the seat, the Horsepower & Heels Thunderbird & I took our maiden launch on February 5th at Phenix Motorsports Park in Phenix City, AL. The objective of the test session was to make some incremental passes and to get me familiar with the car. No biggie, right? Well for some, that would have been no big deal, but for me, anxiety grew everyday that I hadn’t been in a racecar, so I was some nervous about jumping into the seat of a much faster car after so long. Everyone kept telling me “Its like riding a bicycle, Erica. You don’t forget.” Yea… a LOUD, powerful, complicated bicycle.But, as a testimony to the crew and people whom I have in my corner, I am quite proud to admit that the nerves and fear I expected to kick in as I pulled into the burnout for the first time never materialized. Not to say that I’m not overly cautious nor was I prepared for the g’s on that first launch, but at least I wasn’t shakin’ like a polaroid when I finally sat in the seat.
Many people have asked me since that weekend the big questions… What was that first hit like? Well, as much as I have stood behind these things as they leave the starting line, I thought I had a pretty good idea of what that first hit will be like. That was until I let go of that button the first time. As Rick Head said..”I would’ve paid to see your face when you let go of that button the first time.” I assured him it was Priceless.
The weather in Phenix City was cold, so track conditions were not the best due to low track temp. The plan was to start out with some 60′ hits. After the happy shock wore off from that first pass, the second and third went much more smoothly. On the second pass, I managed a 1.09 short time, shutting it off just before the 60′. The third pass I was able to take it out a little futher, but the 60′ was off, and the track conditions were falling off as well. So, we left it at that, and called it a night.
The next weekend, we found a rocker in the valvecover. I am so unaccustomed to this motor, I never heard the miss inside the car. Upon further inspection, Dan found a lifter had failed. Thinking it may have been the result of a potential overwinding in the burnout from my first pass, he replaced the lifters, pushrods, and rockers with fresh pieces to ensure the problem was fixed. Since the temperatures were below freezing last weekend, there was no testing to be had locally. Which meant my next experience would come at my first official event, the ADRL Winter Drags at SGMP in Adel (Valdosta), GA.
With a fixed motor, renewed enthusiasm & great track conditions, I was ready to try and get down broadway and get a feel for navigating the 1/8 mile. Some of my security blanket was unavailable for this weekend, as Dan was in front of me running his own Pro Mod. A few rookie mistakes in the first test passes on Friday made me shut down early (HELLO!?! You’re supposed to leave in 1st gear, not 3rd!) But by the nighttime session, I was ready to kick it on through. Much to my dismay, something went amiss again and I shut off. Back in the pits, it was evident we had some problems by the diaper dragging the ground and the oil accumulation running down the firewall. Kevin and I pulled the turbo/valvecover off to find a rocker off kilter again. The bolt still tight, it was apparent that it had another lifter failure, and with that my weekend was over.
Not exactly how I had hoped to make my Pro Mod debut, but on the bright side, I am confident that once we get these new car bugs figured out, the car will be a very fast piece. I am so tremendously grateful to all the people who have helped me get to this point, and who continue to do so: Mr. Moody, Dan, Kevin, Biscuit, Josh, Dennis, Bill, and everyone else. Unfortunately, this wasn’t the news I was hoping to hear a mere 2 weeks until Orlando, so it is highly unlikely I will make that event. (not enough time to get fixed and sort the 1/4 mile issues before then I fear) That is the downside to not having found any marketing funding, but my hope is that it will come once I get everything sorted out.
In the mean time, its back to work. If I don’t indeed make Orlando, I will be testing at home to get this thing ready to roll in Atlanta. I’ve had a ton of helpful folks depart similar BBF experiences, and have a good idea where to look from here.
Until then…